Pictures

Monday, November 30, 2009

Station 1 Radio Room

The Radio Room project has began. It started with the painting of the walls on Saturday. It will continue for the next several weeks and will hopefully be done by the end of January. It was found that after 15-16 years with no cleaning or painting the walls were dirty. Just the painting helped make the room look better.

Otherwise nothing much has happened in the last few weeks. Our call volume has been relatively slow for the the lasts few weeks compared to the rest of the year. So that is about all that has happened.

Sunday, November 1, 2009

ERV is back at 2

On Sunday ERV or the Emergency Response Vehicle was brought back to station 2 for the winter.

Friday, October 30, 2009

Tomaso's



Last night Tomaso's hosted a thank you dinner for the members of the Cedarburg Fire Department. The food was great and highly appreciated.

Weekend of 10/23

Ran call number 56 out of station 2 on sunday when a crew 4 went on a carbon monoxide call.

Monday, October 12, 2009

Busy Weekend

The past weekend was busy. It began on Friday morning at about 2:30 am when a fire broke out in an apartment above Tomaso's Restaurant. Crews quickly extinguished the fire and contained the fire to one apartment. The people living in the rest of the building were saved by the smoke alarms. The fire only needed a Working Still response do to the location downtown and all of the Volunteers that came. Crews were onscene for 3-5 hours depending what they were assigned to.
After the fire the part to the Clubhouse Gang and Battle Unit 158 and 155 went to Froedert Hospital to do a fire extinguisher training. After getting back from the training some much needed rest was required to recover from the fire.
Later in the day on Friday some of the Clubhouse got together and did some shopping for items that were needed at the station. This also allowed for some driver training on Engine 163. Once back at the station the engine was cleaned for Safety Day.

Safety Day started for the CFD members at 10:30am to set up. The event started at 12:00 pm and lasted until noon. Other than the unusually cold temperatures it was a good event.
On Sunday some of the Clubhouse and Engine 163 went an event for a family in a bad situation. The engine and firefighters hopefully helped lift their spirits. That concluded the the weekend.

Monday, September 28, 2009

162 & 864 Wet Down

On Saturday Engine 162 and Grafton's Engine 864 were ceremonially put into service at Firemen's Park. The event was hosted by the Thiensville FD.

Monday, September 21, 2009

Harvest Fest

The weekend was relatively slow at the Clubhouse. A few house keeping items got done and a lot of sports were watched. The weekend however was ended with a fatal traffic crash at the intersection of Wauwatosa Rd. and Sherman Rd.. More on the crash can be seen on the local news websites. Overall it was quiet.

Saturday, September 12, 2009

A thing called ERV

Well with school starting and the beginning of the football season summer can be declared over. So it's a good time to look back and ponder on what got accomplished at the Clubhouse this summer. For starters many calls have been run out of the station 51 this year about 20 of those came during the summer maybe more. Engine 162 was put together and put into service in four weeks. Engine 163 spent 13 hours in Cudahy
AND... ERV was completed.
The Emergency Response Vehicle was conceived out of the jealousy of Thiensvilles Kuboda. Now some may say that's a little harsh but it is true. Once we all saw Thiensvilles rig we wanted our own. So after many years (about 2) of trying to get a Kuboda just as a joke a deputy Chief found a used Cushman first responder vehicle on craigslist and proposed the idea. However, this idea was taken further then a joke and the price was right $1600. So the membership voted to purchase and effectively resurrect this golf cart for no more then $5000. To get the cart running $700 in batteries was purchased. After spending the beginning of June with the antiques and begin run around the Headquarters complex ERV was taken to Station 2. On the 28th of June the tear down of ERV began. Everything was taken off to be repainted or replaced. Remind you this was Strawberry Fest weekend, the same weekend 162 was put together. After a few weeks of sitting and parts being shipped to different locations the work began again. The frame was grounded, converted, and painted. The picture below shows the finished frame. Around this time we decided to pick an arbitrary date for ERV to be finished which was August 25th.

Once the frame was done the body was ready to go on after being painted professionally.
Picture taken on August 3.
Once the body was on reassembly went quickly. The front was put back on along with the metal rear bumper and metal deck. After the deck and front were put on the windshield and roof columns were reattached. Then the roof and roof rack was mounted. The custom seats came in and were mounted. The stainless steel was polished and mounted with the headlights. The large cabinet and the extinguisher was then mounted next. The front bumper came in and the was mounted after that. By this time the vehicle looked like this.(August 23)
This was the major part of the project but a few things were missing. Like most of the lights. After a few nights of wiring and lifetimes worth of profanities ERV lit up like a paperclip stuck into a wall plug. Picture on August 25th.
At this point the major part of the work was gone and only a few minor things need to be done. On the 26th and 27th the cart was lettered. A few days later the last of the things that could be done were done and we declared ERV done. (September 2nd)
The picture below is the whiteboard which gave us inspiration to get done on time along with a few compliments by the higher powers.
The ERV was taken back to the headquarter complex and shown to the membership at the September business meeting. It's first assignment was on September 11th at the varsity football game. At the game it was actually use for what it was designed to be used for to carry someone injured off the field.

Check Spelling
Facts:
Formerly of Delphi
Scheduled to be finished in the winter (HA!)
Top Speed: 2 MPH uphill; 10 MPH Flat; 15 downhill
Seats 3 and 1 laying
Hours working on it: 200+ with ease through the efforts of many
Cost to taxpayer: $0
Primary functions:
Take patients from areas inaccessible to the rescue squads to an accessible location.
Examples: Strawberry Fest, Forth of July, Football games, Harvest Fest, Interurban Trail
As a side note to all those that believed nothing ever got done at Station N0. 2 or bad things were happening there let this summer prove that the Clubhouse Gang busy doing meaningful work and are not causing trouble.
(sorry for any grammer mistakes but it's late)

Monday, September 7, 2009

Fire in Northwest

A report of a garage fire was called to dispatch Monday night. First responding units arrived on scene to find smoke coming out of the building. The fire was quickly extinguished after crews arrived. The house and garage were cleared of smoke.

Monday, August 31, 2009

Barn Fire

Image by Fox 6


The CFD was call to Newberg today for a barn fire. Engine 161 and 164 responded.

In other news the ERV is 95% complete. Only a few things have to be put on and it will be done.
August has been a relatively slow month compared to July for the CFD. There has been an increase in calls out of Station 2. The total out of Station 2 for the year is 49 calls.

Friday, August 7, 2009

Tuesday, July 28, 2009

In the News

A lot of things have gone on since the last post.

Engine 162- The engine was put into service on the 23rd of July after a majority of the drivers were qualified on it and delivery class was held. The entire process of getting the new truck was completed in about 9 months. The old engine was sold to Denmark, WI and left Cedarburg on the 24th of July.

Cushman- The body was painted and the chassis was prepped for paint. Once everything is painted the assembly should be quick.

Training- A Mass Casualty Incident training was held on the 25th of July at CHS. Multiple departments participated and a lot was learned from it.

Touch-A-Truck- An event was held at Wayne's Drive-in for little kids to see different municiple vehicles and the Clubhouse Gang joined in by bringing Engine 163.

Oh I almost forgot......
We got another structure FIRE.
The call came at 3:00 PM on Monday July 20th. A neighbor reported it since they had smelt something burning and found smoke coming from the house next door. The first crews quickly arrived on scene but were behind from the get go with a strong wind out of the east and a lack of water. Luckly nobody was in the house at the time and a dog was saved. The fire could not have come at a worse time since we were down an engine. Old 162 had already been bought by Denmark and the nobody had pumped the new Engine 162.

The rest of the week should be interesting it is the Ozaukee County Fair this week.

Saturday, July 11, 2009

Task Force 119

On Monday the CFD was part of a MABAS Task Force to help the Cudahy Fire Department at the Patrick Cudahy Plant. Engine 163 was Cedarburg's contribution to the group. The other units in the group were; Mequon Tower, Port Washington Tower and Chief, Thiensville Engine and Chief, Grafton Engine, Saukville Squad. The Task Force met as Mequon Station 2. They left around 6 PM and arrived in staging around 6:30 PM. From that point units were assigned for duty as needed. Engine 163 was assigned to the C-Charlie side of the building around 8:30 PM along with Thiensville. The engine was then shortly assigned to relieve a Cudahy engine in relay pumping. The crew was left for assignment. The crew was assigned to relieve a crew on the roof at around 3-3:30 AM. This assignment included cooling the remaining debris and trying to extinguish the last of fire. At 7:30 AM the crew was relieved and arrived back in Cedarburg at round 8:30 AM.


Time Going Hot: 40 min
On Scene Time: 13 hours
Pumping Time: 7 hours
Gallons of Water Pumped: 400,000-500,000 gallon
Crew Work Time: 4 hours


Another Task Force was scheduled to go back on Wednesday but was called off.

It's not often to be at a fire that gets on the National News.

http://www.hulu.com/watch/81514/nbc-nightly-news-with-brian-williams-fire-shuts-down-milwaukee-meatpacking-plant




Task Force 119 on the way.



The view from staging.

C-Charlie command post.The first assignment.The last area of fire.

The Sunrise

Monday, July 6, 2009

Old 153





Hopefully this works Sent from my iPhone

Monday, June 29, 2009

Strawberry Festival Weekend

This weekend was Strawberry Festival in Cedarburg. So the Clubhouse was staffed on Saturday and Sunday. During the preceding week the new engine arrived and the Cushman was moved to Station 2. The with both vehicles at the Clubhouse thing got done. First on Saturday old 162 and new 162 were placed side by side and all the equipment was mounted on the new truck. Here is a sample of the finished product.

This is the passenger side front compartment.


This is the passenger side rear compartment.
This is the rear compartment

Driver side Rear

Driver side middle

Engineers Compartment

On Sunday some small work was done on 162. The majority of the work done was on the Cushman. The exterior was taken apart and the shell taken off. It will now be cleaned and repainted before assembly.

Friday, June 19, 2009

New Engine 162


Fire!

Shortly after midnight on Wednesday morning a working structure fire was reported. The CFD responded and knocked down the a majority of the fire in the first twenty minutes. Crews then worked on scene for the next four hours. This could be considered a Clubhouse response since a good portions was on the scene but we came from station 1. However 158 did get to the scene. This was the first house fire for the CFD since May of 2008 and the first house fire in the City since 2004.

Wednesday, June 10, 2009

June

The past few weeks have been normal in the amount of calls run by the CFD. However what is unusual has been the lack of fire calls. There has been no more than fifteen calls over a 7 week period. That includes five mutual aid calls. On the other hand the rescue squad is busy as usual.

The Clubhouse has been quiet recently since the lack of calls. Other things have been going on otherwise. Engine 163 got a scene light put on the front of the cab. The station will be the hub of activities involving the new Engine 162 and will be a little more filled then usual. The new engine should arrive sometime next week, hopefully Monday.

Saturday, May 16, 2009

No fire calls in two WEEKS!

There has been no fire calls in two weeks for the CFD. May 2nd was the last call and it was a mutual aid call. It is weird not to have any fire calls in that amount of time. But the rescue squad has been busy.

Saturday, May 9, 2009

Painting

Today the Clubhouse Gang painted the Chief's office.



Sunday, April 26, 2009

Fire Alarm

Engine 163 was first due to an alarm Saturday night. The crew investigated the cause and found out the problem.
This was the twelveth call run out of the Clubhouse in April.

Sunday, April 19, 2009

Brush Fires

Well it has been a while since the last post but that is due mainly to the lack of time there has been to post anything with being busy run to all the brush fires. In 2009 alone there has been more grass fire than in all of 2006, 2007, and 2008 combined, which is not a suprise since there were only about two per year. If my numbers are correct the CFD has extinguished seven this year, but we have been called to at least three other controlled burns. Most of this has occured over the past two weeks. On every fire Battle Unit 158 has rolled from the Clubhouse.
In other news the CFD awards banquet was last night and the Brewers season has started. Other than that not to much has changed lately.

Monday, March 30, 2009

A post was needed

The last two weeks have been slow for the CFD in terms of fire calls. This in turn has meant that the Clubhouse Gang has not run in on a call together for two weekends in a row. The crew did however keep busy by cleaning 154 inside and out, two weekends ago. The leftover time was spent watching basketball.

In other news some interesting dates are coming up:
Wanye's opens Monday, April 6th
Brewers first game is Tuesday, April 7th
Brewers home opener is Friday, April 10th
Summer is on its way! Maybe

Monday, March 16, 2009

Buzzed

Well it was a quiet Sunday for the CHG with no fire calls at all. Not having any fire calls is not a rare thing and is what normally happens. However the day was not lost. We got to sit out front and listen to the Brewers Spring Training game for the second day in a row. Our peace was broken by a rogue pilot of the Civil Air Patrol who thought they were in Top Gun and decided to buzz the station. It was no suprise to us since we saw them coming. That was all the excitement for the day other than doing a little clean up around the station.

Saturday, March 14, 2009

Change of Quarters

Today Engine 163 and Engine 161 did a change of quarters. The CHG did this to give the truck (161) some much needed TLC after a rough winter. The interior was vacuumed, Armor-Alled, windows washed, and floor scrubbed. Nearly every surface in the cab was cleaned. After the interior was done the cab was raised and the batteries checked. The frame was also rinsed off. Before the cab was lowered the placement for the new hammer was located on the bumper. 158 was sent out to go pick up bolts to mount the hammer. While the two on 158 were gone some R&R took place while listening to the Brewers Spring Training game. Since it was a beautiful day the doors were opened and we sat out front. This was short lived since a call came in. 158 was first due from the hardware store with two. 161 was second due with five. Between the two trucks the situation was mitigated and we headed back. Once back at the station the truck had the hammer mounted. A food run was initiated after this and the badminton set was put up outside. After some badminton and food it was time to go home and call it a day. 161 was taken back to Station 1 and 163 brought back to Station 2.

Monday, March 9, 2009

Busy Sunday

Sunday, typically a day in which we get few calls, proved to be the opposite. The CFD ran a total of five calls. The CHG ran on two of the calls. Engine 163 was first due to a call in the heart of the City and was again first due a little while latter on another call in the City. The time not spent on the calls was filled with watching the race. That was easier said then done after coming back from the first call due to a power outage that cut off our cable service. The day could have only been better if the weather had been nice but that was not the case with the wonderful wintry mix we had.

Sunday, March 8, 2009

Saturday Oooh! Oooh!

While the weather was not very nice, the day was still good. The day started a little latter then normal and nothing was done until after the MU game. Once things got going a lot got done. Truck maintenance the done on 163 and 158. 163 was in need of a lot of attention. Both trucks also had tool maintenance done along with SCBA checks on 163. After all the maintenance was done the badminton net was set up. Some mean badminton was played. The recreation was interrupted by a fire call. The Clubhouse Gang was once again first due with Engine 163. Engine 161 also responded. The call was not much of anything and all units were released after about half an hour. Some of the packs on 163 needed to be filled and other supplies were needed so we went to headquarters. After the supply run we headed back to Station 2. After off loading the supplies we installed a new flashlight onto the engine. While this was going on a couple of visitors came the CPD K9 unit. Once we were done with that we ate. Since we had got some new shuttlecocks we decided to test them out. Needless to say they were not up to the challenge of CHGCBL and began to fall apart. This pretty much ended the day and after writing this much, its time to call it a night I need rest.

Monday, March 2, 2009

CHG Projects

The Clubhouse Gang has been assigned with many projects. Some of the projects are minor and need not be listed but the major ones will be listed. Here are a few that come to mind:

-Hospital Recon

-Rural Supply Recon

-Strip and wax Station 2

-Strip and wax park office

-To be announced



I am sure more will be added to the list.



In other news nothing happened on Sunday expect that a new spot for the badmitton court was found.

Sunday, March 1, 2009

The Beginning of CHGCBL

The Clubhouse Gang is beginning a badmiton league. We have know idea on when or who will be competing so CFD members ask if interested.

158 Responds

Battle Unit 158, Squad 153 and 152 all responded to a call Saturday evening. The large number of vehicles that responded was due to the fact that 158 and 153 were out practicing.

Busy Saturday

Saturday saw a lot of things get accomplished. A few of the gang saw a presentation for most of the day. A lot was learned by those that went and the information that was heard will be put to good use. The ones that did not go worked on Engines 161, and 164. The work done on 161 was minimal and entailed mounting a new flashlight. The work done on 164 was substantial and took most of the day. The fan for the compartment vent system had stopped working and needed to be fixed. First access had to be gained to the fan which was mounted in the pump house. This turned out to be relatively easy after a few minutes of wrestling with the aluminum tread plate. After we got in the pump house the fan was quickly removed as you can see in the picture below.





But this was only the beginning of what turned out to be a long project. As it turned out the old PVC piping that was connected to the fan broke off of the pipe going to the other side of the truck. That is what the white tipped pipe on the left hand side is. So it was determined that new pipe had to be installed. That was easier said than done. The pipe that went to the passenger side compartments ended up coming off from its connection and had to be fixed.

In the middle of the picture is where the disconnection occurred. Once this was all done the new PVC could be mounted. Once that was finished the fan was put back into place.



Here you can see the fan being remounted and the hero of the day, Rex. He was the one crawling inside the bowels of 164. The truck was quickly put back together because we had ordered pizza and we were hungry.

After we ate our food we began prepping for the new television in the meeting room by tearing out the shelving that to old one was sitting on and by touch up painting the wall. While this happened a radio was found so that the wash bay could have one. That was the day at Station 1.

Friday, February 27, 2009

Work Week in Review

The past week around the CFD has been relatively slow. The biggest event of the week was Thursday night training. Duty group 3 had their CPR re-certification. Anyone else who showed up to train got to review the 4 gas meter, go through a hose maze, and test their skills in a two minute drill.

Monday, February 23, 2009

The first post

It was a quiet weekend for the Clubhouse Gang with no calls on Saturday or Sunday. However, it allowed for the uninterrupted viewing of the Badgers game and race on Sunday. The events were only watched after all the snow was plowed and shoveled away from the station. Some of the crew investigated a few tools on the engine. Stay tuned for the next post.

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